We pulled everything out again. We refined our ball collector a little and made a small ramp on top for low-scoring. We started working on a gearbox for maximum power. But it caught a lot and shook a lot, which would not work with real robots.
We're gong to have to try another gearbox. This is not good in terms of our process. We're gonna have to try more to make a better plan.
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April 2016
Categories"Uhhh, Guys?"-Scott "YOU ARE TESTING MY PATIENCE" - Daniel "Guys, get to work"-Tom "What should we do???"-Jeff & Eric "GIMME SOMETHING TO DO!!" -Eric "WHAT ARE YOU DOING?!?"-Daniel "Jefferytheengineer" "CLEAN UP CLEAN UP EVERYBODY CLEAN UP" "OMG. ERIC IS ACTUALLY WORKING"- Everyone |